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Post by racket on Jul 13, 2024 20:37:22 GMT -5
Hi Guys
That was an easy fix :-)
Just needed to adjust the bent tip injectors from ~70 degree bend back to ~35 degrees , this projected the spray a little further in and at a shallower angle where it impacts the bore of the evap tube , nothing coming out even when the wall was vertical , hopefully more even turb temps in future :-)
Cheers John
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Post by racket on Jul 21, 2024 20:55:51 GMT -5
Hi Guys
Nice sunny day , the winds have dropped , time for a test run this arvo :-)
Cheers John
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Post by racket on Jul 22, 2024 1:12:11 GMT -5
Hi Guys
Well that was a waste of time and fuel ..............as I accelerate from 3 Bar P2 towards 4 Bar the engine started cutting out , then cut back in as the rpm dropped ,the whole test stand bouncing back and forth , with fuel pressure needle bouncing all over the place as if the P2 over pressure switch was cutting in and out , but it wasn't touched from previous tests , guess I'll need to check it tomorrow.
Thrust was up marginally but temps were also up , so a bit of thinking required on the next step to take .
Cheers John
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Post by racket on Jul 22, 2024 2:43:28 GMT -5
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Post by racket on Jul 22, 2024 17:49:17 GMT -5
P2 overpressure switch checked out OK :-(
Something weird going on ...............LOL, might have been the full moon :-)
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Post by finiteparts on Jul 22, 2024 18:55:11 GMT -5
That looks like it is going into a moderate surge condition.
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Post by racket on Jul 22, 2024 20:57:24 GMT -5
Hi Chris
Yep , had me baffled , still does , all I did was provide more flow area when I had it apart , so surge shouldn't be the issue .
I've still got ~35% of my fuel drums fuel left so it shouldn't have been sucking air either, I really don't have the faintest idea why it started behaving the way it did :-(
I'll keep looking :-)
Cheers John
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praendy2203
Veteran Member
Joined: August 2020
Posts: 183
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Post by praendy2203 on Jul 23, 2024 0:17:59 GMT -5
Hi John,
At 03:12 min in the vid:
3,5 Bar P2, the fuel pressure gauge shows 95 psi and the engine starts to go crazy.
The next time the fuel pressure shows 70 psi and the engine starts to shake.
Its a kind of fuel or combustion problem.
Could it be a flame stall? Cavitation?
Andy
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Post by racket on Jul 23, 2024 4:13:34 GMT -5
Hi Andy
I don't know what has caused it , the only changes I made were a slight mod to the fuel injectors and increased turb exducer clearance by 3mm to provide more flow area so as to increase pressure drop across the NGV, which there was as the NGV exit static pressure reading was lower , 1.5 Bar vs 1.8 previously at 3 Bar P2 , and provide greater impulse energy to the turb wheel to compensate for the exducer clearance , the positives of a radial wheel is the inducer and exducer are two separate entities .
I noticed that the green manometer readings weren't much different than the previous test with the red manometer indicating a bit less dumping of air this test.
Fuel pressures were a lot higher this test, 80 psi vs 65 psi at 3 Bar P2 which would account for the higher turb temps and 15% thrust increase at 3 Bar , even though P4t was lower.
Theres got to be a solution to these variables , just need to figure out what it is :-)
Another test run with a full tank of fuel and some new data collection points maybe ..............I've been also looking at my oil pump pressures which appear to suggest that the pumps power supply is fading a bit too fast, hopefully its not another battery dying :-(
Cheers John
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Post by finiteparts on Jul 23, 2024 8:06:41 GMT -5
The increased clearance should provide more flow assuming similar entry temperatures, but at the cost of turbine efficiency. The increased fuel flow to achieve the same PR suggests that in fact the turbine efficiency has been reduced. You need to turn the wick up to get the power required to achieve the target PR. If you did get more mass flow via the area increase, it may be diminished due to the need to increase the firing temperature. How do the PRs vs RPM look? That may help you understand how the operating point moved in the compressor map space.
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jetric
Veteran Member
Joined: December 2014
Posts: 149
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Post by jetric on Jul 23, 2024 8:17:17 GMT -5
Hi John, Your problem with your engine is the pressure relief valve is opening in the Bosch fuel pump, this is causing the fluctuations in your engine rpm, as you have said you have had to turn the fuel pressure up, you are now hitting the limit of the fuel pump. Richard S. Hi Andy I don't know what has caused it , the only changes I made were a slight mod to the fuel injectors and increased turb exducer clearance by 3mm to provide more flow area so as to increase pressure drop across the NGV, which there was as the NGV exit static pressure reading was lower , 1.5 Bar vs 1.8 previously at 3 Bar P2 , and provide greater impulse energy to the turb wheel to compensate for the exducer clearance , the positives of a radial wheel is the inducer and exducer are two separate entities . I noticed that the green manometer readings weren't much different than the previous test with the red manometer indicating a bit less dumping of air this test. Fuel pressures were a lot higher this test, 80 psi vs 65 psi at 3 Bar P2 which would account for the higher turb temps and 15% thrust increase at 3 Bar , even though P4t was lower. Theres got to be a solution to these variables , just need to figure out what it is :-) Another test run with a full tank of fuel and some new data collection points maybe ..............I've been also looking at my oil pump pressures which appear to suggest that the pumps power supply is fading a bit too fast, hopefully its not another battery dying :-( Cheers John
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Post by finiteparts on Jul 23, 2024 8:19:48 GMT -5
Hopefully you find something else, but that sort of instability really looks like a classic surge condition. Since you did change the operating point, it could have somehow lost surge margin.
It seems like the increase in area, increases flow and that is supported by the slight increase in thrust. If the turbine efficiency goes down, then the PR point for a given speeding should go to a lower PR, higher mass flow point...i.e. away from the surge line.
Maybe when you juice it to get it to accelerate, the transient firing temperature increase pushes you over the surge line. Could maybe test that theory with a very slow accel.
Good luck!
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Post by racket on Jul 23, 2024 17:50:08 GMT -5
Hi Richard
Thanks for the suggestion , so just went and checked the fuel pump and all is normal , took it up to 120 psi without problems , its a 12V pump running on 24V so plenty of grunt , I think I can tick that off as a potential reason.
Bummer , gunna have to keep searching :-(
Cheers John
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Post by racket on Jul 23, 2024 17:59:55 GMT -5
Hi Chris
RPM vs P2 pressures were within a couple of hundred rpm of previous test , well within variables.
The higher jetpipe temps at 3 Bar , ~120 C degrees averaged increase , coupled with the lower P4t ,0.4 vs 0.45 Bar, meant only ~30 ft/sec difference in gas velocity, ~2% , so the 15% thrust increase was mainly from greater mass flow, this would also tie in with the lower NGV exit static pressure as the extra mass flow and higher temps would have needed more pressure drop to get through the throats .
More testing required :-)
Cheers John
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Post by finiteparts on Jul 23, 2024 19:52:46 GMT -5
John, Just a quick estimation of the loss in efficiency due to the increase in the radial clearance based on the data reported here: ntrs.nasa.gov/citations/19700008458Using the last plot on page 19, I took a SWAG at estimating the impact of the 3mm increase. Based on an image of your turbine exit, I estimated the exducer blade span as roughly 40 mm. So the original 1mm diametral clearance (128 -127 mm) was roughly 1.25% of span, while going to the 7mm diametral clearance (134 -127 mm) increases this to roughly 8.75% of span. As plotted below, this data set would estimate somewhere near an 8% loss in turbine total to total efficiency. Just some food for thought. - Chris
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